I replaced the mounts on my QSB5.9-380 by myself, and I used the “raise til it clears” technique. I decided to avoid removing the brackets from the engine because access to some of the bolts would require removing other engine parts. There were no spacers or loose bracket holes to allow a small lift. I needed to lift at least 2 inches. The exhaust connection was removed but nothing else. (Good time to inspect the turbo.)
The most important part is the planning. It is impossible to lift one corner at a time with this approach, so a coordinated lift of the front two and then the rear two (or vice versa) is required. I slightly loosened the non-lifted pair when the other pair was lifted so that the engine could easily pivot on the loose bolts.
I made special screw-type lifting fixtures that were constrained and safe to avoid simple jacking to that height. Every boat will be different so I will not bother to detail my fixtures.
I spent a week pondering and planning, a day making fixtures, and two hours to complete the actual work.
The shaft and coupling alignment is an acquired skill. I will presume the coupling flanges are true and flat. If not, that needs to be corrected before anything else. The other preliminary step (often skipped) is that the shaft needs to be in the correct place. Lengthwise just make sure the prop is located at the correct distance from the final Cutless bearing. Probably the same place it was originally.
Laterally the shaft needs to be in the center of the forward-most bearing or shaft seal. My boat has two well-fitting Cutless bearings so the only thing I needed to do was put slight upward pressure on the shaft at the coupling to counterbalance the weight of the extended shaft and coupling. (I calculated the shaft sag to be about 25 to 30 thousandths)
The other trick for alignment is to use a thin spacer between the coupling faces when adjusting the engine position. I use a spring Pony clamp to lightly hold a 0.015 inch shim between the faces at one point on the perimeter. Then test the gap all around using feelers of about the same 0.015 thickness. Much, much easier than trying to figure out whether a flimsy paper-thin feeler gauge fits or not.
It helps to have good spatial sense to figure out how to move the engine to correct errors seen with the feeler gauges.
The final test is a complete absence of vibration. I did this entire operation twice (used sub-optimal mounts the first time) and was successful both times.
Gene
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