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- Cummins Marine Forum Topics
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Broken Throttle because of misalignment
This topic has 6 replies, has 2 voices, and was last updated by 5 years ago
December 11, 2018 at 4:36 pm The broken throttle that was overtightened is also misaligned. The new cable was attached by a bolt and locknut. This placed the cable in a bind because of the angles. Any suggestions for a proper repair? The throttle is ordered from you and is properly installed. I need help with attaching the cable with correct hardware. Thanks, Retired Diesel Instructor
6 RepliesDecember 14, 2018 at 5:50 am Corey left room for improvement.. I’ll get him to change the page. Tony
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4TBA 3.9 installed in 30 Mainship Throttle Linkage broke
This topic has 4 replies, has 2 voices, and was last updated by 5 years ago
November 24, 2018 at 3:54 pm Throttle linkage broke underway. We patched the link with a tie wrap and piece of wire. Any suggestions on where to find and fix? Any cause you experienced? Thanks!
4 RepliesNovember 25, 2018 at 7:36 am I found I pray is the problem, A cheap made part that was broken on install by a cheap bolt being over tightened. I will order the parts ASAP https://photos.app.goo.gl/jqWdQZoRmqptKJ8PA Thank you and the Seaboard team! Semper Fi!
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SMX-CPK kit for 4BTA3.9M
This topic has 3 replies, has 2 voices, and was last updated by 5 years ago
July 14, 2018 at 9:48 am I have a 1/2 id fuel hose from the tank to primary filter on a dual Racor system. All hose is trident 1/2 id. What fittings would I need to install one of the squeeze bulb kits? The kit would have to tie in with hose. Like the design and appreciate the advice.
3 RepliesJuly 15, 2018 at 6:40 am The fittings are 1/2″npt. The only thing that is 3/8″ is the tubing and squeeze bulb but you’ll be bypassing that for normal running via the valve positions. But you can run the engine via the 3/8″ loop for testing purposes, etc. without issue..
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Broken Throttle because of misalignment