Cummins Marine Diesel Repower Specialists Forums Cummins Marine Engines Aftercooler Maintenance – Results

  • Creator
    Topic
  • #120199

    Stephen Oliver
    Participant
    Vessel Name: Ascella
    Engines: 2x Cummins 330hp Diamond
    Location: Perth, Australia
    Country: Australia

    Hi All

    Thought some may find this interesting.. I have pulled my SB aftercooler from my 6bta 330.. I was actually removing the turbo as I noticed 3 of the 4 bolts holding the riser were sheared off (another post) While removing the turbo I knew the aftercooler was overdue.. so thought why not . I have a week or 2.. so off it came.

    Its been 3 years since I last pulled it.. and at the time the boat was new to me 20 odd years old and i dont think the aftercooler had been pulled prior. The housings were ropey, the cores suspect and generally unloved a fair bit of work got them useable and succeeded pressure testing – following SBmar protocol… alco metalube etc.. .

    Even though I wasnt loving them as much as I should – 3 years is better than never. So I I pumped Rydlyme through it (had some left) to clean the core.. then stripped it. The core took a bit of beating with a lump hammer to get out (I have a machined slab of metal that fits on the shoulder of the core end, to stop damaging it) but looks like it was just the emulsified grease that caused it..

    Housing and core are in no worse shape than 3 years ago and i’m surprised how clean it was.. bear in mind there is no fresh water flush as yet.. (still on the list)

    Its definitely worth using the SBMar protocol for aftercoolers.. makes things so much easier to maintain.

    Steve

    1 user thanked author for this post.
Viewing 2 replies - 1 through 2 (of 2 total)
  • Author
    Replies
  • #120378

    Stephen Oliver
    Participant
    Vessel Name: Ascella
    Engines: 2x Cummins 330hp Diamond
    Location: Perth, Australia
    Country: Australia

    and as an update.. redid everything.

    Pressure test failed. Dropped about 1psi per hour from 25psi on the water side, so pressurised the air side (larger volume) and sealed off the water side, and it equalised the pressure, so definite leak from the core. Tested the core by itself and its a teeny tiny leak (a few teeny bubbles in dishsoap water per seccond) so may have just fractured a solder joint knocking the core out (I need to press them out – i think a tool is needed!)

    So off to get the core resoldered.. šŸ™

    Steve

    1 user thanked author for this post.
    #120371

    Mark Tripi
    Participant
    Vessel Name: Keeper
    Engines: Cummins 4BTA
    Location: Long Island NY
    Country: USA

    Rydlyme is your friend!

Viewing 2 replies - 1 through 2 (of 2 total)

You must be logged in to reply to this topic.